Reduction of NOx emissions from gas turbine combustor with fuel staging

A two stage lean/lean gas turbine combustor was developed with low NOx characteristics in each stage using small radial swirler of 40mm outlet diameter in the pilot stage. Both flame tubes were arranged in series with the smaller combustor (76mm inside diameter) as the pilot stage and the larger...

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Main Author: Mohammad Nazri Mohd.la'afar
Format: Article
Published: 2002
Online Access:http://journalarticle.ukm.my/1392/
http://journalarticle.ukm.my/1392/
id ukm-1392
recordtype eprints
spelling ukm-13922011-10-11T03:45:32Z http://journalarticle.ukm.my/1392/ Reduction of NOx emissions from gas turbine combustor with fuel staging Mohammad Nazri Mohd.la'afar, A two stage lean/lean gas turbine combustor was developed with low NOx characteristics in each stage using small radial swirler of 40mm outlet diameter in the pilot stage. Both flame tubes were arranged in series with the smaller combustor (76mm inside diameter) as the pilot stage and the larger combustor (140mm inside diameter) as the main stage. The pilot stage was fuelled via vane passage fuel injectol; while the main stage was fuelled around the wall of the exit plane of the pilot stage, using wall fuel injectors. Ultra low NOx emissions as low as 15 ppm were obtained when using fuel staging for propane fuel. NOxreduction of 68% was obtained at equivalence ratio of 0.74, when using fuel staging compared to the non-fuel staging tests. This was achieved with small decrease in carbon monoxide emissions and no increase at all in the unburned hydrocarbon emissions at the same equivalence ratio 2002 Article PeerReviewed Mohammad Nazri Mohd.la'afar, (2002) Reduction of NOx emissions from gas turbine combustor with fuel staging. Jurnal Kejuruteraan, 14 . http://www.ukm.my/jkukm/index.php/jkukm
repository_type Digital Repository
institution_category Local University
institution Universiti Kebangasaan Malaysia
building UKM Institutional Repository
collection Online Access
description A two stage lean/lean gas turbine combustor was developed with low NOx characteristics in each stage using small radial swirler of 40mm outlet diameter in the pilot stage. Both flame tubes were arranged in series with the smaller combustor (76mm inside diameter) as the pilot stage and the larger combustor (140mm inside diameter) as the main stage. The pilot stage was fuelled via vane passage fuel injectol; while the main stage was fuelled around the wall of the exit plane of the pilot stage, using wall fuel injectors. Ultra low NOx emissions as low as 15 ppm were obtained when using fuel staging for propane fuel. NOxreduction of 68% was obtained at equivalence ratio of 0.74, when using fuel staging compared to the non-fuel staging tests. This was achieved with small decrease in carbon monoxide emissions and no increase at all in the unburned hydrocarbon emissions at the same equivalence ratio
format Article
author Mohammad Nazri Mohd.la'afar,
spellingShingle Mohammad Nazri Mohd.la'afar,
Reduction of NOx emissions from gas turbine combustor with fuel staging
author_facet Mohammad Nazri Mohd.la'afar,
author_sort Mohammad Nazri Mohd.la'afar,
title Reduction of NOx emissions from gas turbine combustor with fuel staging
title_short Reduction of NOx emissions from gas turbine combustor with fuel staging
title_full Reduction of NOx emissions from gas turbine combustor with fuel staging
title_fullStr Reduction of NOx emissions from gas turbine combustor with fuel staging
title_full_unstemmed Reduction of NOx emissions from gas turbine combustor with fuel staging
title_sort reduction of nox emissions from gas turbine combustor with fuel staging
publishDate 2002
url http://journalarticle.ukm.my/1392/
http://journalarticle.ukm.my/1392/
first_indexed 2023-09-18T19:33:12Z
last_indexed 2023-09-18T19:33:12Z
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